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After many years of continual use and abuse “The Old
Girl”, my 1969 Moto Guzzi V7 Special, needed some major attention. The
electrics were a bit of a mystery with wires stuck in any lug hole that
could be found that could feed power to the required object that needed
electrons to make it go. The motor rattled and clanked but still worked, and
rust was taking over causing the front mudguard and side covers to slowly
disappear. So I decided that what was needed was a headlight to taillight
makeover.
I’d already carried out some work on the bike including
the gearbox and the front suspension. The gear box repairs were rudimentary,
lots of cash and get the hands dirty, whereas the front suspension proved a
bit trickier. The suspension repairs started out as a simple job to fix a
few bits and “She’ll be right” by a mob who gave the job to an apprentice.
On the first ride out, it rained and I discovered that the work done wasn’t
as expected when the front end locked up almost chucking me of the bike.
Zenith Engineering and RAD were employed to rebuild the now
totally stuffed forks back to standard tolerances and fix the left hand fork
boot. Some 30,000+ kms later they are still in good order.
D Day arrived around January 2005 when the bike was
pulled apart in preparation for a well overdue overhaul. How much of an
overhaul was unknown even though some items such as paintwork, brakes, and
electrics were on the agenda, and lots of important questions had to be
answered (and asked) along the way.
In particular the condition of the motor was a shock. The
motor still ran and didn’t blow a lot of smoke even though oil leaked from
just about everywhere. Once the motor was pulled apart we found the front
bearing for the motor was so badly worn that there were grooves in the crank
and you could physically rattle it by hand. In addition, the valve guides
were badly worn, the valves and valve seats were shot, and one head was
cracked. The piston rings were worn, rockers were worn, cam thrust washer
was worn, and the oil pump gears were also worn. Yes, the motor was
technically stuffed! What to do?
Don Newell Motorcycles
provided most of the parts for the motor and what couldn’t be found in
Australia came from Teo Lamers in the Netherlands. Zenith
Engineering was also employed to check and adjust tolerance for the cam,
crank and oil pump once I had completed the preliminary motor rebuild. The
crank had been reground but didn’t need rebalancing because, let’s face it,
the bike is not for racing. But not to skimp, a check of the con rods, and
pistons was carried out to ensure their weights were well within tolerance
on Meredith’s kitchen scales. With the necessary motor parts in hand, crank
reground, heads refurbished, rockers rebuilt, and motor tolerances checked I
put the motor together by March 2006.
What colour scheme? What design? What logo? Painting the
bike was one of my biggest dilemmas. Being a Libran changing my mind is just
part of the game. Fortunately Mark from Queensland Motorcycle Panel and
Paint didn’t completely lose it but instead sat me in his office with a
fist full of colour charts to gaze at. Some colour charts later and checking
out lots of cars and bikes I knew what colour scheme I wanted. The rest is
history and eventually the panels that were broken were rebuilt and the bits
that needed painting were painted by January 2006.
Do I want stainless steel? Do I want chrome? Finding
header pipes and mufflers is not as easy as one might think especially when
you want the same materials throughout to original specifications. I could
get stainless steel header pipes but no stainless steel mufflers. I could
get chromed mufflers but no chromed header pipes. Muffler manufacturers in
Australia wanted a fortune to reconstruct what I had in chromed mild steel
and refused point blank to try and bend stainless steel header pipes to the
original specifications. Pipe manufacturers wanted to make dies for $500 and
an order for some absurd number of header pipes. Eventually after surfing
the net and some general chatting I found what I wanted. Teo Lamers
provided the header pipes in stainless steel for under $100 each landed in
Australia, and Peter H from Gympie, right here in good old Oz,
provided some absolutely immaculate hand made stainless steel mufflers and
clamps manufactured to original specifications for a reasonable price. The
final fitting of the exhaust system was in April 2006.
Did I have everything? Once the basic bike and motor was
back together it was time to locate some of the other bits that were needed.
Teo Lamers was the perfect choice to find wiring looms that fit
straight onto V7, Ambassador, and Eldorado’s cheaper than I could make it
myself. In addition I was able to locate the two front mudguard brackets for
reasonable prices.
The time had arrived to fit some tyres. What tyres to
fit? How do you select a tyre? The decision was made to find a tyre with a
tread that was similar to that of tyres from the 60’s era. Simple it sounds
but not that simple when you realise just how few manufacturers make such a
tyre that fits an 18” wheel. A quick search on the net and it’s AVON to the
rescue and a trip down to Tyres For Bikes to check out availability
and prices. Tyres were purchased and fitted in March 2006.
How do you stop? The original brake shoes were not
completely worn. However, the brakes could slow the bike down but they
couldn’t stop the bike in a fit. 30 years ago finding someone to fit shoes
to brakes was probably an easy thing. These days with disc brakes almost
fitted to everything there aren’t that many people around that want to go
down the old brake shoe road. Once again thanks to Internet technology and
the good old yellow pages phone book I found TBS right here in
Queensland who would do the job and at a good price. The new brake shoes are
a softer compound and the bike now stops as required. The brakes were
refurbished in March 2006.
What to sit on? Sore point this one. Most bikes have a
seat of some kind. Mine had one but still in bits stuck on some shelf in
someone else’s shed. I did get it back after riding there to say g’day
sitting on a cushion. I think the impetus of my visit prompted the quick
response of one sit-on-able seat but not much else. It was quite obvious a
quick search of the Internet was needed to locate a new seat. Harpers
Moto Guzzi in the US provided an LAPD single seat with a matching
luggage rack and pillion pad. The single seat is very comfy and fitted
without alteration - which is a first. The seats and rack were fitted in
June 2006.
What condition are things in? Of course not everything
else was clear sailing. When dismantling the bike it was found that some
threads were badly damaged or worn and some fittings were badly damaged. As
a bit of a side issue Zenith Engineering manufactured the following
items in stainless steel to original specifications: front and rear engine
bolts, engine/frame spacers, front and rear axles, studs for the handle bar
clamps, skid bars for the motor sump, side stand and centre stand spacers
and bolts. These items were manufactured over the rebuild period. In
addition I machined and polished the heads of all stainless steel bolts used
on the bike, sort of give it that finished shiny look.
Is everything alright? Since the rebuild the bike has
successfully completed its first 3,000 kms with no issues other than a seal
leaking around the distributor and a crook generator. A quick trip to a
bearing shop soon located a new O ring to stop that dreaded oil seepage.
Hamilton Auto Electrics were employed to rebuild the generator and to
refurbish the regulator in May 2006 (just before ending up in hospital for
an operation that meant missing out on the Ruptured Budgie Rally).
How on earth do you set things up? The final setup of the
motor was carried out using my eyes, ears and a H2O U tube. The
timing was achieved by setting the crank to 10o by calculating
the degrees per tooth on the flywheel. Once the crank is at 10o I
used a magnifying glass to detect the point gap just starting to open when
twisting the distributor. Don’t smoke so don’t have cigarette papers. Tuning
of the motor was done by running each cylinder as a big single to set air
mixture and initial idle speed. To synchronise the cylinders and final idle
speed I attached a U tube that hangs from the roof of the shed. The U tube
has about 2m of head. I can get the accuracy pretty close to a couple of
Pascal’s from idle up. Like any tune up, a trip up Mt Glorious tests the
timing and the clutch doesn’t slip. A good run out round Esk tests the fuel
economy and engine performance at high speed. While around town tests the
idle when sitting at the lights. The final setup was carried out in June
2006 after an extended and comprehensive run in period.
Where is the key ring? Of course a bike isn’t finished
until you receive that key ring for the key that sits in the ignition from
your loved one. Meredith slaved for hours making a bead key ring with
the letters V7 embroidered. A simple thing? No! Bike trips to the gold coast
and local shops were made to gather a variety of beads in many colours and
sizes. Meredith painstakingly put together many key ring samples until the
perfect colour, size and lettering combination was found to keep me happy.
Of course the key ring has pride of place hanging off the ignition key
sitting in the ignition of the bike up front where I can look at it
regularly.
The bike runs well and is a real treat to own. How many
hours did it take? How much did it cost? Well, I actually can’t tell you
because I don’t actually know. How long is a piece of string? I will say
you will need a decent shed, a buff/polisher, plenty of spare time and
plenty of patience before starting this type of project.
~v7~ |